KATO GS-4 Tsunami install Step by step!

UP_Phill Mar 1, 2008

  1. UP_Phill

    UP_Phill TrainBoard Supporter

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    As we know, the GS-4 has a problem with DCC due to the rear drivers shorting between the pickup frame and motor mount frame. This instruction will describe the installation of a Tsunami Micro sound decoder connected to the light board (modified), with a tender light also fitted. I won't be going down the route of grinding out the driver wells. My fix will be using Kapton tape to insulate them. If you want to grab a dremel and grind out the wells then please head on over to the Atlas N scale forum for related instructions http://forum.atlasrr.com/forum/topic.asp?TOPIC_ID=44730.

    As this instruction will require the complete disassembly of the loco, I advise that only people who have done a few simpler installs attempt this one.

    Tools required:

    Jewelers screw drivers - philips and common
    Sharp hobby knife with new blade
    Meter
    Kapton tape
    Tweezers
    Hack saw...for cutting the tender weight
    File...for cleaning up the tender weight
    Soldering iron with small conical tip
    loco cradle
    Iso alcohol
    ...and a lot of patience!

    Other parts:

    Tsunami Micro TSU-750 (Heavy Steam) decoder
    SP-15R-08 8ohm speaker
    Soundtraxx 1/2" speaker kit PN: 810108
    #32 super-flexible wire PN: N5032 (available from Ngineering)
    SMD leds for the front light board and backup light

    Initially I tested the loco on DC to ensure that it ran smooth. Now for the fun part.

    Disassembly:

    1. Remove smoke box door with light housing - just pulls forward.
    2. Remove boiler shell and cab by lifting the boiler shell where it joins to the cab. You will find that both will come off together. When removing the boiler you'll find that you will need to lift the rear of the boiler quite high to get the front of the boiler past the bell (located on the floor of the pilot).
    3. Remove the bell, Pilot floor, front coupler and cow catcher.

    [​IMG][​IMG]

    4. With the loco upside down remove the ash pan side panels. Be careful that you don't damage any of the piping.
    5. Remove the 4 screws holding the motor frame to the lower pickup frame (2 located center top & 2 located lower rear). Ensure you don't mix up the 2 upper screws with the lower screws which are longer.

    [​IMG]

    6. Remove the front light board then lift the front of the upper frame first then gently lift the rear, sliding the upper frame forward. It should separate from the lower frame quite easily. You will also find that the tender will disconnect from the loco. Remove the drive worm retaining clip, then gently ease the drive plus universal out of the drive tower.

    [​IMG]
     
  2. UP_Phill

    UP_Phill TrainBoard Supporter

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    7. Now remove the skirt assembly by lifting the rear of the assembly while wriggling the front of the assembly over the light tower.

    [​IMG]

    8. You now end up with the upper assembly with motor. It's now just a matter of cleaning the driver wells with alcohol, letting them dry and covering the affected areas with Kapton tape. The following photo shows the driver wells with Kapton tape applied.

    [​IMG]

    9. You now need to test the mod. Temporarily replace the upper frame (without the skirt assy) onto the lower frame. Whilst compressing the rear drivers, ensure that there is no connectivity between the wheel flanges and upper frame. Also check for no connectivity when moving the drivers from side to side. Once you are happy with this it's time to reassemble.

    [​IMG]
     
  3. UP_Phill

    UP_Phill TrainBoard Supporter

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    Reassembly:

    Reassembly is generally the reverse of the above.

    1. Replace the skirt assy by angling it over the light tower.

    2. Refit the upper frame to the lower frame by sliding the rear of the frame under the rear of the skirt. You will have to spread the skirt sides a bit to get the upper frame sitting flush with the lower.

    3. Reattach the tenders dual draw bars. You will have to spread the rear of the frames to insert the draw bars. I sometimes wish I had another pair of hands!

    4. Tighten the 2 (short) upper screws and 2 (longer) lower screws. Don't forget the plastic washers.

    You should end up with this:

    [​IMG]

    [​IMG]

    5. Refit the worm and universal assembly. I found this to be a bit tricky, but using a pair a bent nose tweezers to align the universal while seating the 2 bearing blocks eventually had the little bugger back where should be. Now refit the worm cover...just snaps in.

    Light Board

    As I don't want to run more then 2 extra wires from the tender to the loco, I decided that modifying the light board would be the way to go. The Tsunami in the tender will only control the upper Mars light, while the lower will stay connected to the rails. I also replaced the orange SMD leds with white items.

    The light board mod was relatively easy to accomplish. I first de-soldered both SMD leds and replaced them with the new white items. I then de-soldered the large IC located near the front of the, then cut the trace going from the center pad on the underside of the board. This left me with a couple of nice pads to solder the decoder leads to.

    Modified board

    [​IMG]

    Cut this trace on the underside

    [​IMG]
     
    Last edited by a moderator: Mar 1, 2008
  4. UP_Phill

    UP_Phill TrainBoard Supporter

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    Next step is to remove the molded on posts in the tender

    [​IMG]

    Then cut down the weight cradle so the the speaker assembly can be fitted. I also removed about 3/4 of the metal weight.

    [​IMG]

    Here's the tender with speaker and decoder to work out component placement.

    [​IMG]



    ......to be continued.
     
    Last edited by a moderator: Mar 1, 2008
  5. Lownen

    Lownen TrainBoard Member

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    Incredible! Thank you.
     
  6. UP_Phill

    UP_Phill TrainBoard Supporter

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    Now, on to the juicy part!

    Solder 2 wires to the middle and right solder pads of the light board. Thread the 2 wires back along the frame, then through the 2 motor brush openings. Carefully route the wires down the rear of the frame out towards the tender.

    [​IMG]

    [​IMG]

    I'm utilising the original Kato analogue power board in the tender to transfer track and motor power to the decoder. First thing to do is drill out the 2 holes in the board. This is to cut continuity from the lower traces to the upper. Next thing to do is to file 2 notches in the fwd portion of the board to allow the track pick up wires to thread through.

    [​IMG]




    ......to be continued.
     
  7. UP_Phill

    UP_Phill TrainBoard Supporter

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    Carefully refit the power board ensuring that none of the wires get caught. This is how it looks prior to the weight cradle being refitted.

    [​IMG]

    Drill a 5mm hole in the cradle just to the rear of the steel weight. This will enable the wires to be threaded from the board through the weight cradle into the tender.

    [​IMG]

    Insert all of the wires ensuring that the 2 fwd headlight don't get mixed up with the black track connection. You'll have to move the wires around to ensure that the cradle sits flush with the tender frame.

    [​IMG]


    In the photo above you will see 2 pieces of PCB which are glued to the top of the steel weight. One with 6 pads and one with 2. In Aus we call this bread board, I assume that other countries have a similar product. This allows me to remove the decoder without having pull the entire tender apart.

    Solder the red and black wires to the first 2 pads on the bread board, followed by the orange and gray leads on pads 3 and 4.

    I soldered 2 purple wires to the speaker then sealed it and the speaker enclosure with silicone. Attach the assy to the rear floor of the tender with some double sided tape and run the wires forward, soldering them to the PCB.

    The 2 black headlamp wires are soldered to the smaller PCB.

    Next, cut the red, black, orange and gray decoder leads leaving 1.25" Solder these leads to the corresponding pads on the PCB.

    Cut the blue lead from the decoder ensuring that it has enough length to reach the small PCB. Using the discarded blue wire, twist and solder it to the blue wire you just cut. Solder the 2 joined blue wires to the headlight pad on the small PCB and run the longer one back to the rear of the tender. ( I hope this makes sense?) Solder the white wire with a dropping resistor to the headlight pad on the small PCB.

    Solder the 2 purple speaker leads to their corresponding pads

    Last but not least is the rear tender light. I used a small peice of bread board with 2 tracks. I soldered an SMD led across the 2 tracks with a dropping resistor also soldered to one of the tracks. I then connected the decoders blue and yellow leads to this assy.




    Continued next post.
     
    Last edited by a moderator: Mar 1, 2008
  8. UP_Phill

    UP_Phill TrainBoard Supporter

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    These last 2 images show the installed decoder with the rear tender light also installed.

    [​IMG]

    [​IMG]

    Test the newly installed decoder on the programming track, ensuring that you get a good decoder read.

    Re-assemble the loco boiler, cab and pilot details, replace the tender shell and customise the programming to you needs.

    This would have to be one of the longest but extremely enjoyable installs I have ever done. The Tsunami sounds incredible, even with the small 1/2" speaker.
     
  9. Silverexpress

    Silverexpress TrainBoard Member

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    Just curious to know if the Tsumani will fit in the tender if placed directly on top of the weight. You stated post #4 that you cut 3/4 of the weight, if so have you noticed any issues with derailments or the decoder resetting due to lost of track contact? In retrospect do you suppose it will fit with the weight as is?
     
  10. UP_Phill

    UP_Phill TrainBoard Supporter

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    I did a test fit of the decoder mounted on top of the weight but found that the tender shell wouldn't fully sit down on to the chassis. I've countered the loss of weight by adding moldable tungsten just forwd of the speaker assy.
     
  11. UP_Phill

    UP_Phill TrainBoard Supporter

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    Amendment: As I was lowering the tender shell, I found that the speaker assembly was a tad to tall! When I did the test fit I didn't take into account the thickness of the foam double sided tape...duh! Anyway the fix was pretty easy. Just lay the speaker assembly on its side and glue a small styrene post on the center rear of the tender chassis to support the backup light.
     
  12. Westfalen

    Westfalen TrainBoard Member

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    Phill, have you had any problems with the Micro Tsunamis overheating? I've installed three in different locos, (Challenger, MP pacific and On30 4-4-0) and all get so hot, (too hot to hold between your fingers), after a couple of minutes running that they cut out and have to be let cool down.
     
  13. UP_Phill

    UP_Phill TrainBoard Supporter

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    No problems at all. My 4yr old ran it for around an hour and a half last night pulling the daylight....it ran perfectly. I did notice that the tender shell is warm but that is to be expected. Both my Challengers (one with Tsunami & the other with MRC) get warm after a couple of hours running.
     
  14. Silverexpress

    Silverexpress TrainBoard Member

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    Westfalen,

    Do you have your Tsumani's connected to lights? If so are you limiting the current going to those lights by the use of resistors? If so, what values are the resistors? The Micro-Tsunami's have a 0.75 amp limit. That includes motor and any other function you throw in - like lights.
     
  15. TrainGuy

    TrainGuy Advertiser

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    Tsunami current draw

    The current draw on the GS4 is about .2-.5 amp. If you are hooking up 2 LEDS they draw about 20ma ea. This is well within the Tsunami range.
    We have done a lot of Tsunami's in the Kato GS4's and while the decoder does get warm it has never shut down or too hot to the touch.
    Vince
    TopHobbyTrains
     
  16. Westfalen

    Westfalen TrainBoard Member

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    Thanks for the input on the overheating problem, looks like I'm the only one having it, but the three I've installed in three different locos and run on five different Digitrax command stations and power supplies all do it. I'd ruled out headlights drawing too much current as the MP Mike's headlight is not connected to the decoder and sound volume is turned down to the minimum. I'll have to experiment further.
     
  17. TrainGuy

    TrainGuy Advertiser

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    Did you contact SoundTraxx about the issue? Maybe they can shed some light. I have had good luck speaking with them.
     
  18. DSZ&N

    DSZ&N TrainBoard Member

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    WOW I need a drink after that tear down. I can't thank you enough UP_phil I would have broken something for sure without your write up. On the plus side I know what a ash box is now :) . A couple of things for people reading this and thinking about it. All the pieces above the front coupler come of by lifting upward. I used a small screwdriver and slowly rotated the blade back and forth.
     
  19. Tom Schilling

    Tom Schilling TrainBoard Member

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    Westfalen, I'm having the same problem but in kind of a different situation. I just installed a micro in a small old time passenger car. The speaker is in a mail car just ahead of the decoder car. I've connected the motor wires, orange and gray, to a 1/2 watt, 100 OHM resistor to simulate a motor draw. The deocder works just fine but it gets too hot and, after about a minute and a half, the sound drops out. The locomotive keeps running for another two minutes and the sound starts up again.

    I've posed the problem to some experts including Soundtraxx and am waiting to hear back. I may need a different sized resistor or some other magic electronic fix. I know absolutely nothing about this stuff. ...Tom
     
  20. Tom Schilling

    Tom Schilling TrainBoard Member

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    Westalen, an update, for what its worth. I got some advice from Bruce Pretarca at Litchfield Station. He suggested that once the DSX-like Tsunami was programmed, disconnect the resistor. I did. And, he asked me to make sure the decoder was sitting on the plastic bottom of the car so that the plastic would act like a heat sink. Mine was sitting on double sided tape. I removed the tape as well. I haven't had an overheat problem since. The latter advice might apply to you. Hope this helps. ...Tom
     

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