Great, thanks. It is only the "stop" which does this, the off button does not. I am also getting: [Nextion] Display of page 1 was not successful....
I have a little more time and I am back playing with this again. After going through the thread I have switched to using the development branch...
Yep thinking along these lines myself. I was just waiting to see what the final cost would be of the boards. Probably getting 5 or more of the...
Just to add I most impressed by the work you have done Atani on this. Makes my progress on my throttle look a bit pathetic. I am still working...
I need to have a look at the LCC Specs. It has been twenty odd years since I was doing this and there is a lot of new and interesting new...
With using a WROVER32-U you can have an external aerial if you put the PCB in a case. Would look nice and tidy. I may have missed this but why do...
Yes this not working then working without changing anything is really frustrating me. Will be interesting to see what luck I have with the next...
I ran the system for a bit. From the logfile: [MotorBoard.cpp:58] powerOff(): [OPS] Disabling DCC Signal [MotorBoard.cpp:58] powerOff(): [PROG]...
I was only using the verose logging to see if I can track down why the prog side was not working. Though this might not be much use if it...
On timer this was missing from the DEBUG output on the development branch. [DCCSignalGenerator_Timer.cpp:55] enable(): [OPS] Configuring Timer(1)...
Ok. Trying this again. With the decoders it is the motor control side which is damaged the other functions still work. So I can use them for...
Regarding easy of use of this project. There is an issue in that moving from the Arduino IDE to VSCode + PlatformIO (which is what I use) due to...
Still get some issues with the decoder detection in the development branch. But will wait to until you push out the next version. I notice you...
Ok I used the value 3072 and the throttle for the first time is working both in the web interface and JRMI. No crashes now. If I set it to 0...
I thought I had posted this earlier. I am still working on getting this working reliably. However while I can successfully now read the decoder...
Ahh yes we finally have both LED's Working and the logfile [MotorBoard.cpp:176] powerOnAll(): Enabling DCC Signal for all boards...
Log file below. Not sure if it really shows anything useful. [WiFiInterface.cpp:161] begin(): Waiting for WiFi to connect...
Yes I am just using all the defaults at the moment to try and keep things as simple. It is the fact the LES B49 and me are using different ESP32...
Ok. I have now added a 7.5v supply for the ESP32 UNO board. Rechecked the two jumpers powered up and the same issue. I am wondering if there is...
I have the jumpers in place. Though I did not use a separate power supply. I will add that tomorrow and test it again. I would like to see if I...